RENEWED ENTHUIASM?
Back in November 2011 I had started to think about the fitting of the kick start leaver. Was the original shaft really as bad as I thought? I had a go at fitting the leaver to the shaft and tried to tighten the pinch bolt. No matter how hard I tried I couldn't stop the leaver moving on the shaft. This wouldn't do and to cut the leaver to help improve the grip was not acceptable as it would potentially destroy a good kick start leaver.
I reluctantly came to the conclusion that the shaft should be changed (something that should have happened during the rebuild of the engine). Patrick agreed to send me a new shaft (£36) so I could check that it fitted on my leaver, if no better than the original one I could return the new shaft and decide what to do next. As soon as it arrived I fitted it to the leaver and was relieved to find it fitted much better
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original shaft |
Not too surprising when you look at the difference between the splines at the end of the shafts. The old one has certainly seen better days
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new shaft |
Having shown that it would be worth fitting a new shaft it only remained to fit it.
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